Very well said, consumers are gullible, and the more marketing the easier to reel them in. The ones being looked at by the OP are not a set and forget SVB's they have to be worked by the operator to extract the best out of them.
Over here in Australia it is illegal not to carry spare parts for the product being sold I would have thought it would be a similar law in the UK.
Should bonded elements burn out the replacement is the kettle and the elements then transfer the pump, circuit board and screen over.
Magical Pancake who is a forum member made a video of replacing the element.
The wash of water running over the element is just another gimmick, the scorching happens not in the boil but in the mash, mashing at a lower wattage eliminates scorching. The turbulence of the boil prevents sugars from sticking to the bottom plate.
Stirring regularly during the mash maintains the temperature, doesn't matter if it is a PID or analog temperature controller. Whatever unit is purchased will take the effort on the user's part to get the best out of it.
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The scorching happens not in the boil but in the mash" is certainly not what happened on my first use of BZ gen 4 35l. My first brew ever, destined to go down the sink.
A Weisenbock, with 7.5kg malts, 50% wheat malt, in 23l mash.
Virtually stuck step mash, extremely slow recirculation, even with lots of stirring. During boil, built in sensor was showing 115°C, then got an 'overheat shutdown' for a minute.
On draining found most of bottom covered with thick burnt on layer, almost up to bottom of diffuser plate. And a smokey tasting wort, that was very astringent.
It seems all the stirring let flours through. And with the slow recirculation, these largely settled on the base, rather than being recirculated and caught back in the grain bed.
On second brew (Budvar, no wheat) recircirculation was fine at max flow.
Before boil, I'd drained off the mash to check the base was clear, and found there were just a few small patches of flour. But, as it was a lager, I rinsed these off to be sure the flour didn't scorch.
This time, initial recircilulation (to 40 minutes) was done around outside of the malt pipe, rather than through the malt. Acheived by sticking the recirculation pipe through one of the lifting holes. The malt was then being heated from all round, as well as from below, and putting bubble wrap over the lid reduced heat loss from it's top.
Using the Rapt probe thermometer, about my favourite improvement to the BZ, showed how effective 'outside' recirculation was. Over the first 10 minutes, with no recirculation, temperature near top centre of bed had dropped 1°C. After starting side circulation, top-centre temperature started climbing around 0.5 °C a minute.
When using a Rapt probe, the BZ controls the real mash temperature much better. The 'differential override' setting, sets how much higher the bottom temperature (measured by internal sensor) can go above the set temp.
With diff set to 5°C, and say a 60°C target, you can see how quickly the base temperature overshoots the target, even at 40% power, then oscillates between 59°C and around 65°C. And how slowly, depending on recirculation rate and diff setting, the real temperature slowly climbs to the target.
The probe thermometer doesn't help much during sparge; boil; or cooling, and would be in the way. But once probe is powered down, the BZ switches back to using its internal sensor.
I'd been wondering if the stuck Weisenbock mash, might have been from starting recirculation through bed too early. Rather than the (notorious) wheat malt being the problem (despite 10% oat husks).
Same grains re-ordered, so hope to find out soon.